NTSB Says Bolts on Boeing Jetliner Were Missing Before Panel Blew Out in Midflight Last Month

NTSB Says Bolts on Boeing Jetliner Were Missing Before Panel Blew Out in Midflight Last Month
This photo released by the National Transportation Safety Board shows the door plug from Alaska Airlines Flight 1282 on Monday, Jan. 8, 2024, in Portland, Ore. A panel used to plug an area reserved for an exit door on the Boeing 737 Max 9 jetliner blew out Jan. 5, shortly after the flight took off from Portland, forcing the plane to return to Portland International Airport. (National Transportation Safety Board via AP)
The Associated Press
2/6/2024
Updated:
2/6/2024

Bolts that helped secure a panel to the frame of a Boeing 737 Max 9 were missing before the panel blew off the Alaska Airlines plane last month, according to accident investigators.

The National Transportation Safety Board (NTSB) issued a preliminary report on the Jan. 5 incident Tuesday.

The report included a photo from Boeing, which worked on the panel, which is called a door plug. In the photo, three of the four bolts that prevent the panel from moving upward are missing. The location of the fourth bolt is obscured.

The investigators said that the lack of certain damage around the panel indicates that all four bolts were missing before the plane took off from Portland, Oregon.

Pilots were forced to make a harrowing emergency landing with a hole in the side of the plane.

Without the bolts, nothing prevented the panel from sliding upward and detaching from “stop pads” that secured it to the airframe.

The preliminary report said the door plug, installed by supplier Spirit AeroSystems, arrived at Boeing’s factory near Seattle with five damaged rivets around the plug. A Boeing crew replaced the damaged rivets, which required them to remove the four bolts to open the plug.

The NTSB did not declare a probable cause for the accident—that will come at the end of an investigation that could last a year or longer.

“Whatever final conclusions are reached, Boeing is accountable for what happened,” CEO David Calhoun said in a statement. “An event like this must not happen on an airplane that leaves our factory. We simply must do better for our customers and their passengers.”

Investigators said they were still trying to determine who authorized the Boeing crew to open and reinstall the door plug.

The fuselage plug area of Alaska Airlines Flight 1282 Boeing 737-9 MAX, which was forced to make an emergency landing with a gap in the fuselage, is seen during its investigation by the National Transportation Safety Board (NTSB) in Portland, Ore., on Jan. 7, 2024. (NTSB/Handout via Reuters)
The fuselage plug area of Alaska Airlines Flight 1282 Boeing 737-9 MAX, which was forced to make an emergency landing with a gap in the fuselage, is seen during its investigation by the National Transportation Safety Board (NTSB) in Portland, Ore., on Jan. 7, 2024. (NTSB/Handout via Reuters)

Safety experts have said the accident could have been catastrophic if the Alaska jet had reached cruising altitude. The decompression in the cabin after the blowout would have been far stronger, and passengers and flight attendants might have been walking around instead of being belted into their seats.

The incident has added to questions about manufacturing quality at Boeing that started with the deadly crashes of two Max 8 jets in 2018 and 2019, killing 346 people.

The Federal Aviation Administration (FAA) is investigating whether Boeing and its suppliers followed proper safety procedures in manufacturing parts for the Max. The FAA has barred Boeing from speeding up production of 737s until the agency is satisfied about quality issues.

FAA Administrator Michael Whitaker said Tuesday that his agency is about halfway through a six-week audit of manufacturing processes at Boeing and its key supplier on the Max, Spirit AeroSystems. He said the agency is confronted with two questions—what’s wrong with the Max 9, and “what’s going on with the production at Boeing?”

Spirit AeroSystems, which Boeing spun off as a separate company nearly 20 years ago, said in a statement that it was reviewing the NTSB preliminary report and was working with Boeing and regulators “on continuous improvement in our processes and meeting the highest standards of safety, quality, and reliability.”

By David Koenig